Spillway for Little Goose Dam, Snake River, Washington
Author: Richard L. Johnson
Publisher:
Published: 1975
Total Pages: 132
ISBN-13:
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Author: Richard L. Johnson
Publisher:
Published: 1975
Total Pages: 132
ISBN-13:
DOWNLOAD EBOOKAuthor:
Publisher:
Published: 1975
Total Pages: 0
ISBN-13:
DOWNLOAD EBOOKThe spillway for Little Goose Dam, designed to pass discharges up to 850,000 cfs (2125 cfs per ft of crest), was studied in a 1:42.47-scale, 3-bay, sectional model and a 1:100-scale general model to investigate the performance of various elements of the structure and to determine flow conditions in the tailrace. Maximum velocities that fluctuated between 5 and 12 fps along the north embankment upstream from the spillway were indicated by the spillway model. Tests indicated that the stilling basin of original design was not satisfactory. An acceptable stilling basin was developed in the model, but unusual artesian flow at the site would have required a costly drainage system to protect the basin slab against uplift. Sixteen roller bucket plans were investigated in efforts to eliminate the basin slab and drainage system. A modified Angostura-type bucket, with simpler teeth and shorter apron, was adopted.
Author:
Publisher:
Published: 1975
Total Pages: 0
ISBN-13:
DOWNLOAD EBOOKThe spillway for Little Goose Dam, designed to pass discharges up to 850,000 cfs (2125 cfs per ft of crest), was studied in a 1:42.47-scale, 3-bay, sectional model and a 1:100-scale general model to investigate the performance of various elements of the structure and to determine flow conditions in the tailrace. Maximum velocities that fluctuated between 5 and 12 fps along the north embankment upstream from the spillway were indicated by the spillway model. Tests indicated that the stilling basin of original design was not satisfactory. An acceptable stilling basin was developed in the model, but unusual artesian flow at the site would have required a costly drainage system to protect the basin slab against uplift. Sixteen roller bucket plans were investigated in efforts to eliminate the basin slab and drainage system. A modified Angostura-type bucket, with simpler teeth and shorter apron, was adopted.
Author:
Publisher:
Published: 1983
Total Pages: 80
ISBN-13:
DOWNLOAD EBOOKAuthor: Richard L. Johnson
Publisher:
Published: 1975
Total Pages: 160
ISBN-13:
DOWNLOAD EBOOKAuthor: Walla Walla District Corps of Engineers
Publisher:
Published: 1963
Total Pages:
ISBN-13:
DOWNLOAD EBOOKAuthor: Walla Walla District Corps of Engineers
Publisher:
Published: 1964
Total Pages:
ISBN-13:
DOWNLOAD EBOOKAuthor: M. M. Kubo
Publisher:
Published: 1983
Total Pages: 76
ISBN-13:
DOWNLOAD EBOOKUnderwater inspection of the Little Goose Dam roller bucket and tailwater channel following about 10 years of operation revealed foundation erosion around various structures and the end of the bucket. A 1:50-scale movable-bed model was used to evaluate the effect of high spillway discharges on the erosional tendencies in the tailwater channel. Studies were accomplished to establish the most desirable spillway operating schedule which would flush the riverbed material and debris from the roller bucket.
Author: M. M. Kubo
Publisher:
Published: 1983
Total Pages: 14
ISBN-13:
DOWNLOAD EBOOKAuthor: United States. Army. Corps of Engineers. Walla Walla District
Publisher:
Published: 1963
Total Pages:
ISBN-13:
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